| Download | - View final version: Pressure loss tests on a second model of a turbine volute (PDF, 4.4 MiB)
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| DOI | Resolve DOI: https://doi.org/10.4224/40003764 |
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| Author | Search for: Bassett, R. W.1; Search for: Murphy, C. L.1 |
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| Affiliation | - National Research Council Canada. Division of Mechanical Engineering
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| Format | Text, Technical Report |
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| Physical description | 20 p. |
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| Abstract | This report presents the results of continued tests made on a second low-pressure model of a tip turbine volute duct having an axial discharge; this volute is different from the previous model in passage size and re-entry arrangement.
The over-all pressure loss, including the discharge nozzles, was measured and found to be 22 percent of the total gauge pressure in the supply duct. The tests indicated that 8. 9 percent was lost in the volute duct, representing 26. 7 percent of the dynamic head.
The static pressure along the inner and outer duct walls suggested that a free vortex velocity distribution existed in the duct and that the loss of static pressure was similar to that occurring along the walls of a straight pipe. |
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| Publication date | 1962-08 |
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| Publisher | National Research Council Canada |
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| Series | |
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| Language | English |
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| Peer reviewed | No |
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| Export citation | Export as RIS |
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| Report a correction | Report a correction (opens in a new tab) |
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| Record identifier | 0a504133-ad07-4bd9-ac59-babc188e18b9 |
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| Record created | 2025-10-01 |
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| Record modified | 2025-11-03 |
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