| Téléchargement | - Voir la version finale : An evaluation of the acoustic performance of No. 3 cell inlet silencer (PDF, 4.3 Mio)
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| DOI | Trouver le DOI : https://doi.org/10.4224/40003910 |
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| Auteur | Rechercher : Weibust, T.1; Rechercher : Macaula, G. A.1 |
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| Affiliation | - Conseil national de recherches Canada. Établissement aéronautique national
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| Format | Texte, Mémorandum |
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| Description physique | 12 p. |
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| Résumé | As part of a programme designed to reduce the jet noise Emitted from the Engine Laboratory, a baffle-type silencer was installed in the inlet to No. 3 test cell. The purpose of this investigation was to evaluate the transmission loss across the silencer, as well as the resulting noise reduction at a point 30 feet in front of the inlet. Because there was no engine in the cell at the time of installation, the silencer was tested using an 1 1/8-inch-diameter air jet as noise source. Some time after completion however, a few rough over-all sound -pressure measurements were made with an Olympus engine in the cell. |
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| Date de publication | 1957-04-10 |
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| Maison d’édition | National Research Council Canada |
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| Série | |
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| Langue | anglais |
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| Publications évaluées par des pairs | Non |
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| Identificateur | NAE-361 |
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| Exporter la notice | Exporter en format RIS |
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| Signaler une correction | Signaler une correction (s'ouvre dans un nouvel onglet) |
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| Identificateur de l’enregistrement | aaf0cec3-adc7-4e32-8bcb-c053ee0091ff |
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| Enregistrement créé | 2025-11-28 |
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| Enregistrement modifié | 2025-11-28 |
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